The Marfy blouse, my personal challenge for January, is coming together. After creating my own pattern from the pieces Marfy supplied, I was ready to make a toile (or wearable muslin) to test my construction method and make any necessary fitting adjustments.
For the toile, I chose a woven fabric from my stash that I wasn’t particularly attached to. That way, if things work out, I’ll wear it. If they don’t, I haven’t wasted special or expensive material. The striped heart pattern isn’t my usual taste, but I do like the red and white combination. Also, it might be fun to wear on Valentine’s Day.
Before I even cut into the fabric, I made notes on to sew it together. I update my notes as I go along. When I’m done, I’ll have a good set of instructions to put in the envelope with the pattern.
After washing, it was obvious that the hearts fabric was pretty flimsy. I knew it would need interfacing to give it some structure, especially in the collar and button bands. I had four different possibilities on hand, so I made test swatches of each of them to see what worked best (or if I needed to get something else).
- Pellon SF101 Shape Flex , woven fusible: the winner. Provided nice support without stiffness.
- Pellon 950F ShirTailor, non-woven fusible: too crisp. This one would be better for heavier fabric, men’s shirts and cuffs, etc.
- Pellon 845F Designer’s Lite, non-woven fusible: very lightweight interfacing kept the fabric from fraying and losing shape, but added no stiffness at all. Better for silky fabrics or the body of the garment (not the collar).
- Heat n’ Bond Lightweight, non-woven fusible: very similar support to SF101. This one would have also worked well, but since I had more of the Pellon on hand, I went with that.
Since the original Marfy pattern pieces have no seam allowance, they are ready to use as pattern pieces for interfacing.
Section by section, I assembled the parts of the blouse. I left out the pockets but otherwise kept to the design. I saved a little time by using the serger to overcast the raw edges instead of doing any “nice” seam finishes. As the parts started to come together, I pinned them to my duct-tape double. Once all of the components were prepared (collar, back, yoke/sleeve, and fronts), I was able to get a good idea of how the final version would fit. Some of the things I checked were the position of the darts, whether the side seams fell straight down or not, and where the hem should fall for a comfortable length.
I had expected to adjust the darts, which I did. What I didn’t expect was that I would need to let out the bottom so much. Apparently my posterior does not conform to Italian standards – who knew? Because I needed to let out more than my seam allowance would allow, I went ahead and drafted an entirely new back pattern piece. After making another back section from the new pattern, I pinned it in place on my double.
Well, it was better, but not good. I needed to pinch away about an inch horizontally across the small of the back. I made yet another pattern piece and tried again. Ideally, I would also take out a little from the center seam, but I was concerned that the stripe pattern would look too distorted if I did that. So, I went with version 3 and moved on.
Once I was done with the back, I needed to adjust the front a little bit by adding side darts.
One thing I wasn’t able to test-fit on the double was the sleeve. I had to wait until the body of the blouse was complete to see how much gathering I would need. I frequently need to adjust sleeves for myself, so I knew I didn’t want to commit to the bias tape edge until I was sure the fit would work.
The instructions for the sleeve edges were a little mysterious. The sleeve was not pictured in detail on the illustration. The pleated parts were clearly marked on the pattern, but the only detail about how to handle the sleeve edges was “Reduce to cm.” There was a pencilled in (!) number 8.5 near it. Reduce 8.5 cm? One side? Both sides? Reduce to 8.5cm? I had to guess. I measured the edge of both sleeve pieces on each side. I ran a couple rows of gathering stitches and pulled the bobbin threads until the total edge measurements were reduced by 17 cm in total (8.5 for the front, 8.5 for the back). I basted the gathers, then tested for fit. It seemed a little snug, so I let them out until I was happy, then sewed on my matching self-made bias.
The final sleeve looks pretty good, but dips a little too low. Unfortunately, there wasn’t any good way to raise the bottom of the sleeve opening once the pieces had been cut, so I did not incorporate that necessary modification to the toile. I did adjust the pattern pieces, though.
The collar was next. Finally, something that just worked!
Then it was time for the part I was dreading: the buttonholes. My buttonhole skills are improving, but they are far from perfect. But I think these will do unless there is a close inspection. The buttons are just old ones I found in my stash, except for the top button. I thought it would be cute to put a little red heart button at the top, so I did. I could have probably put a row of hearts down the front, but it was getting a little too cute for a grown woman already!
The blue line in center of the buttonhole is where I marked the buttonhole placement using water-soluble marker. It comes right out with water – you can take it off with a damp rag in a pinch.
I turned up a simple blind machine hem and pronounced it done!
I’m really glad I made a test version. Now I can cut into my “good” fabric with confidence. And I may even wear the test version for more than just Valentine’s Day.
Here are some pictures of me wearing my “wearable muslin.” Click the images to enlarge.
Missed Part 1? You can find it here: Marfy Blouse 1: The Pattern
Next time: Marfy Blouse 3: Pulling it all Together